浙江电力

2017, v.36;No.255(07) 53-55+62

[打印本页] [关闭]
本期目录(Current Issue) | 过刊浏览(Archive) | 高级检索(Advanced Search)

600MW超临界机组干态深度调峰能力试验研究
Experimental Investigation of Dry-state Deep Peak Regulation Capacity of 600 MW Supercritical Unit

董利斌,李泉,杨程,郑植
DONG Libin,LI Quan,YANG Cheng,ZHENG Zhi

摘要(Abstract):

介绍了某发电厂600 MW超临界机组深度调峰TOP优化系统逻辑设计、稳态和动态试验的情况,试验探索了在TOP平台投入下、机组协调运行中,发电厂600 MW超临界本生直流锅炉机组的干态最低负荷可达200 MW(小于35%)。试验证明机组在干态条件下即完成深度调峰要求。
The paper introduces logic design of TOP optimization system for deep peak regulation as well as steady-state and dynamic tests of 660 MW supercritical unit in a power plant. The tests explore that the minimum dry-state load of 660 MW supercritical Benson once-through boiler can reach up to 200 MW(less than35%) with the operation of TOP platform and coordinated operation of unit. The tests show that deep peak regulation can be implemented under dry state.

关键词(KeyWords): 深度调峰;TOP系统;逻辑;试验;干态;低负荷;超临界
deep peak regulation;TOP system;logic;test;dry state;low load;supercritical

Abstract:

Keywords:

基金项目(Foundation):

作者(Author): 董利斌,李泉,杨程,郑植
DONG Libin,LI Quan,YANG Cheng,ZHENG Zhi

DOI: 10.19585/j.zjdl.201707013

扩展功能
本文信息
服务与反馈
本文关键词相关文章
本文作者相关文章
中国知网
分享